spi: cadence: fix clock imbalance on probe failure

Make sure that the controller is active before disabling clocks on probe
failure to avoid unbalanced clock disable.

Also drop the usage count before returning (so that the controller can
be suspended after a probe deferral) and restore the autosuspend
setting.

Fixes: d36ccd9f7e ("spi: cadence: Runtime pm adaptation")
Cc: stable@vger.kernel.org	# 4.7
Cc: Shubhrajyoti Datta <shubhrajyoti.datta@xilinx.com>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://patch.msgid.link/20260421123615.1533617-3-johan@kernel.org
Signed-off-by: Mark Brown <broonie@kernel.org>
This commit is contained in:
Johan Hovold
2026-04-21 14:36:13 +02:00
committed by Mark Brown
parent 5b1689a41f
commit ecea4f0e9d

View File

@@ -741,7 +741,6 @@ static int cdns_spi_probe(struct platform_device *pdev)
/* Set to default valid value */
ctlr->max_speed_hz = xspi->clk_rate / 4;
xspi->speed_hz = ctlr->max_speed_hz;
pm_runtime_put_autosuspend(&pdev->dev);
} else {
ctlr->mode_bits |= SPI_NO_CS;
ctlr->target_abort = cdns_target_abort;
@@ -752,12 +751,17 @@ static int cdns_spi_probe(struct platform_device *pdev)
goto clk_dis_all;
}
if (!spi_controller_is_target(ctlr))
pm_runtime_put_autosuspend(&pdev->dev);
return ret;
clk_dis_all:
if (!spi_controller_is_target(ctlr)) {
pm_runtime_disable(&pdev->dev);
pm_runtime_set_suspended(&pdev->dev);
pm_runtime_put_noidle(&pdev->dev);
pm_runtime_dont_use_autosuspend(&pdev->dev);
}
remove_ctlr:
spi_controller_put(ctlr);