If a command is queued to the final usable TRB of a ring segment, the
enqueue pointer is advanced to the subsequent link TRB and no further.
If the command is later aborted, when the abort completion is handled
the dequeue pointer is advanced to the first TRB of the next segment.
If no further commands are queued, xhci_handle_stopped_cmd_ring() sees
the ring pointers unequal and assumes that there is a pending command,
so it calls xhci_mod_cmd_timer() which crashes if cur_cmd was NULL.
Don't attempt timer setup if cur_cmd is NULL. The subsequent doorbell
ring likely is unnecessary too, but it's harmless. Leave it alone.
This is probably Bug 219532, but no confirmation has been received.
The issue has been independently reproduced and confirmed fixed using
a USB MCU programmed to NAK the Status stage of SET_ADDRESS forever.
Everything continued working normally after several prevented crashes.
Link: https://bugzilla.kernel.org/show_bug.cgi?id=219532
Fixes: c311e391a7 ("xhci: rework command timeout and cancellation,")
CC: stable@vger.kernel.org
Signed-off-by: Michal Pecio <michal.pecio@gmail.com>
Signed-off-by: Mathias Nyman <mathias.nyman@linux.intel.com>
Link: https://lore.kernel.org/r/20241227120142.1035206-4-mathias.nyman@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Improve dbc transfer rate performance by copying the received data to
the tty buffer directly in the request complete callback function if
possible.
Only defer it in case there is already pending deferred work, tty is
throttled, or we fail copy the data to the tty buffer
The request complete callback is already called by a workqueue.
This is part 3/3 of a dbc performance improvement series that roughly
triples dbc performace when using adb push and pull over dbc.
Max/min push rate after patches is 210/118 MB/s, pull rate 171/133 MB/s,
tested with large files (300MB-9GB) by Łukasz Bartosik
Cc: Łukasz Bartosik <ukaszb@chromium.org>
Signed-off-by: Mathias Nyman <mathias.nyman@linux.intel.com>
Link: https://lore.kernel.org/r/20241227120142.1035206-3-mathias.nyman@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Queue event polling work with 0 delay in case there are pending transfers
queued up. This is part 2 of a 3 part series that roughly triples dbc
performace when using adb push and pull over dbc.
Max/min push rate after patches is 210/118 MB/s, pull rate 171/133 MB/s,
tested with large files (300MB-9GB) by Łukasz Bartosik
First performance improvement patch was commit 31128e7492
("xhci: dbc: add dbgtty request to end of list once it completes")
Cc: Łukasz Bartosik <ukaszb@chromium.org>
Signed-off-by: Mathias Nyman <mathias.nyman@linux.intel.com>
Link: https://lore.kernel.org/r/20241227120142.1035206-2-mathias.nyman@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If the transfer is cancelled due to a disconnect or driver tear down
(error code -ESHUTDOWN), then just free the command. However, if it got
cancelled due to other reasons, then send a sense CHECK CONDITION status
with TCM_CHECK_CONDITION_ABORT_CMD status to host notifying the delivery
failure. Note that this is separate from TASK MANAGEMENT function abort
task command, which will require a separate response IU.
See UAS-r04 section 8.
Signed-off-by: Thinh Nguyen <Thinh.Nguyen@synopsys.com>
Link: https://lore.kernel.org/r/f2ae293c1fc39df4d242a2f724584bf4ec105ece.1733876548.git.Thinh.Nguyen@synopsys.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Currently the default bMaxBurst is 0. Set default bMaxBurst to 15 (i.e.
16 bursts) to Data IN and OUT endpoints to improve performance. It
should be fine for a controller that supports less than 16 bursts. It
should be able to negotiate properly with the host at packet level for
the end of burst.
If the controller can't handle a burst of 16, and high performance isn't
important, the user can use BOT protocol from mass_storage gadget driver
instead.
Signed-off-by: Thinh Nguyen <Thinh.Nguyen@synopsys.com>
Link: https://lore.kernel.org/r/9d6265db4d138e542f281988362bc4392b034d43.1733876548.git.Thinh.Nguyen@synopsys.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The UDC state in sysfs (/sys/class/udc/<udc>/state) should accurately
reflect the current state of the USB Device Controller.
Currently, the UDC state is not handled consistently during gadget
disconnection. While the disconnect interrupt path correctly sets the
state to "not-attached", manual deconfiguration leaves the state in
"configured", misrepresenting the actual situation.
This commit ensures consistent UDC state handling by setting the state to
"not-attached" after manual deconfiguration. This accurately reflects the
UDC's state and provides a consistent behavior regardless of the
disconnection method.
Signed-off-by: Roy Luo <royluo@google.com>
Reviewed-by: André Draszik <andre.draszik@linaro.org>
Tested-by: André Draszik <andre.draszik@linaro.org>
Link: https://lore.kernel.org/r/20241223042536.1465299-1-royluo@google.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Fixes issue where memory will fail to be allocated for larger bulk
transfers, ~1 MB or more. This occurs because userland libraries, such
as libusb, send the entire USB data buffer when SG support is detected.
The assumption is that the driver knows how to properly split the data
up before sending it out.
By hardcoding a limit, bigger transfers that exceed the SG tablesize
limit of 32 will be unable to use SG. This results in an attempt to
allocate contiguous pages which, unsurprisingly, will fail too and
returns an ENOMEM. It looks like other drivers that support SG allow for
any length of SG lists. Accepting any SG size allows the driver to
properly handle large bulk transfer situations.
Tested bulk read and write operations using the following devices:
- Logitech Webcam Pro 9000 - USB 2.0
- SanDisk Ultra - USB 3.0
- Logitech M500s Mouse
Signed-off-by: Jason Long <jasonlongball@gmail.com>
Reviewed-by: Shuah Khan <skhan@linuxfoundation.org>
Link: https://lore.kernel.org/r/20241218161344.202637-1-jasonlongball@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This commit adds a new AMS for responding to a "Get_Revision" request.
Revision message consists of the following fields:
+----------------------------------------------------+
| Header | RMDO |
| No. of data objects = 1 | |
+----------------------------------------------------+
While RMDO consists of:
* B31..28 Revision Major
* B27..24 Revision Minor
* B23..20 Version Major
* B19..16 Version Minor
* B15..0 Reserved, shall be set to zero.
As per the PD spec ("8.3.3.16.2.1 PR_Give_Revision State"), a request is
only expected when an explicit contract is established and the port is
in ready state. This AMS is only supported for PD >= 3.0.
Signed-off-by: Amit Sunil Dhamne <amitsd@google.com>
Reviewed-by: Badhri Jagan Sridharan <badhri@google.com>
Link: https://lore.kernel.org/r/20241210-get_rev_upstream-v2-3-d0094e52d48f@google.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add support for parsing "pd-revision" DT property in TCPM and store PD
revision and version supported by the Type-C connnector.
It should be noted that the PD revision is the maximum possible revision
supported by the port. This is different from the 2 bit revision set in
PD msg headers. The purpose of the 2 bit revision value is to negotiate
between Rev 2.X & 3.X spec rev as part of contract negotiation, while
this is used for Get_Revision AMS after a contract is in place.
Signed-off-by: Amit Sunil Dhamne <amitsd@google.com>
Reviewed-by: Badhri Jagan Sridharan <badhri@google.com>
Link: https://lore.kernel.org/r/20241210-get_rev_upstream-v2-2-d0094e52d48f@google.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The TI HD3SS3220 Type-C controller supports configuring
its role preference when operating as a dual-role port
through the SOURCE_PREF field of the General Control Register.
The previous driver behavior was to set the role preference
based on the dr_set typec_operation.
However, the controller does not support swapping the data role
on an active connection due to its lack of Power Delivery support.
Remove previous dr_set typec_operation, and support setting
the role preference based on the corresponding fwnode property,
as well as the try_role typec_operation.
Signed-off-by: Oliver Facklam <oliver.facklam@zuehlke.com>
Reviewed-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Link: https://lore.kernel.org/r/20241211-usb-typec-controller-enhancements-v3-3-e4bc1b6e1441@zuehlke.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The TI HD3SS3220 Type-C controller supports configuring the port type
it will operate as through the MODE_SELECT field of the General
Control Register.
Configure the port type based on the fwnode property "power-role"
during probe, if present. If the property is absent, leave the
operation mode at the default, which is defined by the PORT pin
of the chip.
Support configuring the port type through the port_type_set
typec_operation as well.
The MODE_SELECT field can only be changed when the controller is in
unattached state, so follow the sequence recommended by the datasheet to:
1. disable termination on CC pins to disable the controller
2. change the mode
3. re-enable termination
This will effectively cause a connected device to disconnect
for the duration of the mode change.
Signed-off-by: Oliver Facklam <oliver.facklam@zuehlke.com>
Reviewed-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Link: https://lore.kernel.org/r/20241211-usb-typec-controller-enhancements-v3-2-e4bc1b6e1441@zuehlke.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This commit addresses an issue related to below kernel panic where
panic_on_warn is enabled. It is caused by the unnecessary use of WARN_ON
in functionsfs_bind, which easily leads to the following scenarios.
1.adb_write in adbd 2. UDC write via configfs
================= =====================
->usb_ffs_open_thread() ->UDC write
->open_functionfs() ->configfs_write_iter()
->adb_open() ->gadget_dev_desc_UDC_store()
->adb_write() ->usb_gadget_register_driver_owner
->driver_register()
->StartMonitor() ->bus_add_driver()
->adb_read() ->gadget_bind_driver()
<times-out without BIND event> ->configfs_composite_bind()
->usb_add_function()
->open_functionfs() ->ffs_func_bind()
->adb_open() ->functionfs_bind()
<ffs->state !=FFS_ACTIVE>
The adb_open, adb_read, and adb_write operations are invoked from the
daemon, but trying to bind the function is a process that is invoked by
UDC write through configfs, which opens up the possibility of a race
condition between the two paths. In this race scenario, the kernel panic
occurs due to the WARN_ON from functionfs_bind when panic_on_warn is
enabled. This commit fixes the kernel panic by removing the unnecessary
WARN_ON.
Kernel panic - not syncing: kernel: panic_on_warn set ...
[ 14.542395] Call trace:
[ 14.542464] ffs_func_bind+0x1c8/0x14a8
[ 14.542468] usb_add_function+0xcc/0x1f0
[ 14.542473] configfs_composite_bind+0x468/0x588
[ 14.542478] gadget_bind_driver+0x108/0x27c
[ 14.542483] really_probe+0x190/0x374
[ 14.542488] __driver_probe_device+0xa0/0x12c
[ 14.542492] driver_probe_device+0x3c/0x220
[ 14.542498] __driver_attach+0x11c/0x1fc
[ 14.542502] bus_for_each_dev+0x104/0x160
[ 14.542506] driver_attach+0x24/0x34
[ 14.542510] bus_add_driver+0x154/0x270
[ 14.542514] driver_register+0x68/0x104
[ 14.542518] usb_gadget_register_driver_owner+0x48/0xf4
[ 14.542523] gadget_dev_desc_UDC_store+0xf8/0x144
[ 14.542526] configfs_write_iter+0xf0/0x138
Fixes: ddf8abd259 ("USB: f_fs: the FunctionFS driver")
Cc: stable <stable@kernel.org>
Signed-off-by: Akash M <akash.m5@samsung.com>
Link: https://lore.kernel.org/r/20241219125221.1679-1-akash.m5@samsung.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There's USB error when tegra board is shutting down:
[ 180.919315] usb 2-3: Failed to set U1 timeout to 0x0,error code -113
[ 180.919995] usb 2-3: Failed to set U1 timeout to 0xa,error code -113
[ 180.920512] usb 2-3: Failed to set U2 timeout to 0x4,error code -113
[ 186.157172] tegra-xusb 3610000.usb: xHCI host controller not responding, assume dead
[ 186.157858] tegra-xusb 3610000.usb: HC died; cleaning up
[ 186.317280] tegra-xusb 3610000.usb: Timeout while waiting for evaluate context command
The issue is caused by disabling LPM on already suspended ports.
For USB2 LPM, the LPM is already disabled during port suspend. For USB3
LPM, port won't transit to U1/U2 when it's already suspended in U3,
hence disabling LPM is only needed for ports that are not suspended.
Cc: Wayne Chang <waynec@nvidia.com>
Cc: stable <stable@kernel.org>
Fixes: d920a2ed86 ("usb: Disable USB3 LPM at shutdown")
Signed-off-by: Kai-Heng Feng <kaihengf@nvidia.com>
Acked-by: Alan Stern <stern@rowland.harvard.edu>
Tested-by: Jon Hunter <jonathanh@nvidia.com>
Link: https://lore.kernel.org/r/20241206074817.89189-1-kaihengf@nvidia.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When device_add(&udev->dev) succeeds and a later call fails,
usb_new_device() does not properly call device_del(). As comment of
device_add() says, 'if device_add() succeeds, you should call
device_del() when you want to get rid of it. If device_add() has not
succeeded, use only put_device() to drop the reference count'.
Found by code review.
Cc: stable <stable@kernel.org>
Fixes: 9f8b17e643 ("USB: make usbdevices export their device nodes instead of using a separate class")
Signed-off-by: Ma Ke <make_ruc2021@163.com>
Reviewed-by: Alan Stern <stern@rowland.harvard.edu>
Link: https://lore.kernel.org/r/20241218071346.2973980-1-make_ruc2021@163.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>